We have been working on our robot in the past few days since Dallas. We had several problems with our launcher at event when ever you put it out for a real match. It just wasn’t consistent.
It was pretty easy getting the prototype working and we should be able to do the final make over, quickly on Friday at Lone Star. We did have to play around with launch geometry but it wasn’t that complicated. We also looked pulse timing and we found we can change our shot pretty easily using it.
“Perfection is not attainable, but if we chase perfection we can catch excellence.” – Vince Lombardi